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AS-B885-101
检测到系统错误:EEPROM
校验和错误
参数\u SigLatched位29
检测到E 546B 3系统错误:EEPROM
校验和错误(LLDP MIB数据)
参数\u SigLatched位29
E 546C 0 EEPROM文件不可用
检测到E 5500 3系统错误:超时
数据传输期间
E 5501 4检测到系统错误:已接收
切换位不匹配
软件看门狗安全
模块eSM(CPU\U A)
检测到E 5502 2系统错误:超时
读/写请求期间
检测到E 5503 2系统错误:无效
在以下情况下的响应:
读/写请求
E 5504 4检测到系统错误:安全
模块不可用
E 5505 4检测到系统错误:
不确定的安全类型
单元
E 5506 1写入访问期间检测到错误
通过现场总线连接至安全模块
(附加信息=详细错误
代码)
E 5507 3未处理故障复位
通过安全模块eSM
安全模块eSM为
无法执行故障
重置,例如,因为
它仍在处理错误
回答
触发故障复位
再一次
E 5600 3电机连接相位错误
检测
参数\u SigLatched位26
缺少电机相位。验证电机的连接
阶段。
E 5603 3检测到换向错误
参数\u SigLatched位26
电机接线错误
缆绳
编码器信号丢失或
受到干扰。
负载扭矩更大
大于电机扭矩。
编码器EEPROM
包含不正确的数据
(编码器相位偏移为
不正确)。
电机未调整。
验证电机相位,验证
编码器接线。
改进EMC,验证
接地和屏蔽
联系
使用不同大小的
能够承受
负载扭矩。
验证电机数据。
联系技术支持。
E 6102 4检测到系统错误:内部
软件错误
参数\u SigLatched位30
E 6103 4检测到系统错误:系统
堆栈溢出
参数\u SigLatched位31
E 6104 0检测到系统错误:除法
零(内部)
检测到E 6105 0系统错误:溢出
32位计算期间(内部)
E 6106 4检测到系统错误:大小
数据接口不匹配
参数\u SigLatched位30
E 6107 0参数超出值范围
(检测到计算错误)
E 6108 0功能不可用
System error detected: EEPROM checksum error Parameter _SigLatched Bit 29 E 546B 3 System error detected: EEPROM checksum error (LLDP MIB data) Parameter _SigLatched Bit 29 E 546C 0 EEPROM file not available E 5500 3 System error detected: Timeout during transmission of data E 5501 4 System error detected: Received toggle bit does not match Software watchdog safety module eSM (CPU_A) E 5502 2 System error detected: Timeout during read/write request E 5503 2 System error detected: Invalid response in the case of a read/write request E 5504 4 System error detected: Safety module not available E 5505 4 System error detected: Indeterminable type of safety module E 5506 1 Error detected during write access to safety module via fieldbus (additional info = detailed error code) E 5507 3 A Fault Reset was not processed by the safety module eSM The safety module eSM was unable to execute the Fault Reset, for example, because it was still processing an error response. Trigger the Fault Reset again. E 5600 3 Motor connection phase error detected Parameter _SigLatched Bit 26 Missing motor phase. Verify connection of motor phases. E 5603 3 Commutation error detected Parameter _SigLatched Bit 26 Incorrect wiring of motor cable. Encoder signals are lost or subject to interference. The load torque is greater than the motor torque. The encoder EEPROM contains incorrect data (encoder phase offset is incorrect). Motor is not adjusted. Verify motor phases, verify encoder wiring. Improve EMC, verify grounding and shield connection. Use a differently sized motor that can withstand the load torque. Verify the motor data. Contact Technical Support. E 6102 4 System error detected: Internal software error Parameter _SigLatched Bit 30 E 6103 4 System error detected: System stack overflow Parameter _SigLatched Bit 31 E 6104 0 System error detected: Division by zero (internal) E 6105 0 System error detected: Overflow during 32 bit calculation (internal) E 6106 4 System error detected: Size of data interface does not match Parameter _SigLatched Bit 30 E 6107 0 Parameter outside of value range (calculation error detected) E 6108 0 Function not available
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